CROUCH PETRO CO inactive
OP #190940 · Since 1981-12-07· P-5: Active
1715 WEST 58TH, AMARILLO
Spud Rate
6%
2 of 31 (6mo+)
Median Spud Days
118
p25-p75: 70-166d
Cancel Rate
3%
1 cancelled
Expired Undrilled
28
Avg Permits / Yr
5
Spud Momentum: inactive ⓘBased on wells spudded in the last 6 months compared to the prior 6 months. Active Years: 6 Horizontal: 0% Top County: JACK
Window: | Type:
Permits (1yr)
0
vs Prior
0%
Counties (1yr)
0
Avg Depth (1yr)
--
Hz % (1yr)
0%
All Time
31
Basins (1yr): Barnett / North Texas, Panhandle / Haynesville
Depth Range (1yr): 2,600 - 8,000 ft
Current Portfolio (RRC scheduling system)
Total Wells
1
On Schedule
0
Producing
0
Shut In
0
Acquired
0
from other operators
Divested
5
to other operators
Counties
HANSFORD 1
Fields
CLEMENTINE (MORROW UPPER) 1
Cum Oil: 7,444 BBL Cum Gas: 133,773 MCF
Wells Operated (1)
| API | LEASE | FIELD | COUNTY | STATUS | SCHED |
|---|---|---|---|---|---|
| 42-195-30163 | VENNEMAN | CLEMENTINE (MORROW UPPER) | HANSFORD | — | N |
Production History
Permit History (all operated wells, latest 15)
View all →| SOURCE | PERMIT | API | TYPE | LEASE | COUNTY | ISSUED | FROM/TO |
|---|---|---|---|---|---|---|---|
| divested | 230531 | 42-179-31580 | DRILL | YOES | GRAY | 1984-02-27 | to: CROUCH PETROLEUM COMPANY |
| divested | 161993 | 42-155-30321 | DRILL | MORRIS COMPANY | FOARD | 1982-05-27 | to: ROJO ENERGY |
| divested | 161878 | 42-155-30317 | DRILL | MORRIS | FOARD | 1982-05-26 | to: BLACKBRUSH O & G LLC |
| divested | 161877 | 42-155-30316 | DRILL | MORRIS | FOARD | 1982-05-17 | to: BLACKBRUSH O & G LLC |
| divested | 161880 | 42-155-30319 | DRILL | MORRIS | FOARD | 1982-05-17 | to: MB EXPLORATION LLC |
Permit Activity
No data available