DEAN ENGY, INC inactive
OP #208872 · Since 1997-02-28· P-5: Active
P O BOX 10155, MIDLAND
Spud Rate
67%
8 of 12 (6mo+)
Median Spud Days
54
p25-p75: 45-69d
Cancel Rate
0%
0 cancelled
Expired Undrilled
4
Avg Permits / Yr
1
Spud Momentum: inactive ⓘBased on wells spudded in the last 6 months compared to the prior 6 months. Active Years: 14 Horizontal: 0% Top County: MIDLAND
Window: | Type:
Permits (1yr)
0
vs Prior
0%
Counties (1yr)
0
Avg Depth (1yr)
--
Hz % (1yr)
0%
All Time
12
Basins (1yr): Eagle Ford / Maverick, Permian (West), Permian (East)
Depth Range (1yr): 3,500 - 11,000 ft
Current Portfolio (RRC scheduling system)
Total Wells
1
On Schedule
0
Producing
0
Shut In
0
Acquired
0
from other operators
Divested
7
to other operators
Counties
UPTON 1
Fields
SPRABERRY (TREND AREA) 1
Cum Oil: 555,303 BBL Cum Gas: 0 MCF
Wells Operated (1)
| API | LEASE | FIELD | COUNTY | STATUS | SCHED |
|---|---|---|---|---|---|
| 42-461-30288 | MCCUISTION COMMUNITY HOSPITAL | SPRABERRY (TREND AREA) | UPTON | — | N |
Production History
Permit History (all operated wells, latest 15)
View all →| SOURCE | PERMIT | API | TYPE | LEASE | COUNTY | ISSUED | FROM/TO |
|---|---|---|---|---|---|---|---|
| divested | 695495 | 42-461-36748 | DRILL | NEAL HEIRS | UPTON | 2010-05-05 | to: PIONEER NATURAL RES. USA INC. |
| divested | 624841 | 42-329-32131 | RECOMP | MARALO 32 | MIDLAND | 2006-08-24 | to: XTO ENERGY INC. |
| divested | 603789 | 42-329-32154 | RECOMP | BABB 30 | MIDLAND | 2005-08-18 | to: XTO ENERGY INC. |
| divested | 602812 | 42-329-32152 | RECOMP | BABB 30 | MIDLAND | 2005-06-30 | to: XTO ENERGY INC. |
| divested | 534419 | 42-371-37308 | DRILL | STOCKTON A | PECOS | 2003-07-21 | to: REIN PUSHER OPERATING LLC |
| divested | 527863 | 42-371-37243 | DRILL | STOCKTON A | PECOS | 2003-01-29 | to: REIN PUSHER OPERATING LLC |
| divested | 459318 | 42-371-36689 | DRILL | STOCKTON A | PECOS | 1997-02-28 | to: REIN PUSHER OPERATING LLC |
Permit Activity
No data available