NOLTE, MIKE E inactive
OP #612553 · Since 1987-04-29· P-5: Active
PO BOX 341, LONGVIEW
Spud Rate
0%
0 of 3 (6mo+)
Median Spud Days
--
Cancel Rate
0%
0 cancelled
Expired Undrilled
3
Avg Permits / Yr
1
Spud Momentum: inactive ⓘBased on wells spudded in the last 6 months compared to the prior 6 months. Active Years: 3 Horizontal: 0% Top County: HARRISON
Window: | Type:
Permits (1yr)
0
vs Prior
0%
Counties (1yr)
0
Avg Depth (1yr)
--
Hz % (1yr)
0%
All Time
3
Basins (1yr): East Texas
Depth Range (1yr): 7,032 - 10,900 ft
Current Portfolio (RRC scheduling system)
Total Wells
2
On Schedule
0
Producing
0
Shut In
0
Acquired
2
from other operators
Divested
3
to other operators
Counties
GREGG 1
MARION 1
Fields
HARLETON NORTH-EAST (PETTIT) 1
WILLOW SPRINGS (COTTON VALLEY W) 1
Cum Oil: 0 BBL Cum Gas: 135,685 MCF
Wells Operated (2)
| API | LEASE | FIELD | COUNTY | STATUS | SCHED |
|---|---|---|---|---|---|
| 42-315-30664 | BUCKINGHAM | HARLETON NORTH-EAST (PETTIT) | MARION | — | N |
| 42-183-30455 | RACHFORD J. H. | WILLOW SPRINGS (COTTON VALLEY W) | GREGG | — | N |
Production History
Permit History (all operated wells, latest 15)
View all →| SOURCE | PERMIT | API | TYPE | LEASE | COUNTY | ISSUED | FROM/TO |
|---|---|---|---|---|---|---|---|
| divested | 370677 | 42-203-30242 | RECOMP | GOOCH GAS UNIT NO. III | HARRISON | 1990-04-11 | to: KING OPERATING CORPORATION |
| divested | 359437 | 42-183-30460 | RECOMP | HENDERSON, JOHN | GREGG | 1989-07-17 | to: BUFFCO PRODUCTION INC. |
| divested | 329487 | 42-203-30196 | RECOMP | LANE, WILLIAM H. | HARRISON | 1987-04-29 | to: KING OPERATING CORPORATION |
| acquired | 266450 | 42-315-30664 | DRILL | THOR ENERGY/ BUCKINGHAM | MARION | 1985-02-08 | from: THOR ENERGY OF LOUISIANA, INC. |
| acquired | 94153 | 42-183-30455 | DRILL | RACHFORD, J. H. | GREGG | 1980-09-19 | from: DALCO PETROLEUM U.S., LTD. |
Permit Activity
No data available