RUBICON EXPL CO inactive
OP #732307 · Since 1984-04-17· P-5: Active
4016 SOUTH BETTER DRIVE, DALLAS
Spud Rate
0%
0 of 6 (6mo+)
Median Spud Days
--
Cancel Rate
0%
0 cancelled
Expired Undrilled
6
Avg Permits / Yr
1
Spud Momentum: inactive ⓘBased on wells spudded in the last 6 months compared to the prior 6 months. Active Years: 6 Horizontal: 0% Top County: SHACKELFORD
Window: | Type:
Permits (1yr)
0
vs Prior
0%
Counties (1yr)
0
Avg Depth (1yr)
--
Hz % (1yr)
0%
All Time
6
Basins (1yr): Eagle Ford / Maverick
Depth Range (1yr): 1,999 - 4,700 ft
Current Portfolio (RRC scheduling system)
Total Wells
1
On Schedule
0
Producing
0
Shut In
0
Acquired
1
from other operators
Divested
5
to other operators
Counties
SHACKELFORD 1
Fields
ROARK (TANNEHILL) 1
Cum Oil: 4,321 BBL Cum Gas: 0 MCF
Wells Operated (1)
| API | LEASE | FIELD | COUNTY | STATUS | SCHED |
|---|---|---|---|---|---|
| 42-417-36434 | NAIL 135 | ROARK (TANNEHILL) | SHACKELFORD | — | N |
Production History
Permit History (all operated wells, latest 15)
View all →| SOURCE | PERMIT | API | TYPE | LEASE | COUNTY | ISSUED | FROM/TO |
|---|---|---|---|---|---|---|---|
| divested | 358142 | 42-417-37263 | DRILL | NAIL 150 E-1 | SHACKELFORD | 1989-04-20 | to: FTC CONSULTING LLC |
| divested | 350052 | 42-417-37194 | DRILL | NAIL 150F | SHACKELFORD | 1988-08-12 | to: ROBICAN EXPLORATION CO. |
| divested | 348718 | 42-417-37186 | DRILL | NAIL 150F | SHACKELFORD | 1988-07-13 | to: RUBICON EXPLORATION COMPANY |
| divested | 337692 | 42-417-37114 | DRILL | NAIL 150E | SHACKELFORD | 1987-10-21 | to: FTC CONSULTING LLC |
| divested | 325268 | 42-367-33027 | DRILL | FLOYD, JAMES W. | PARKER | 1987-01-13 | to: RUBICON EXPLORATION COMPANY |
| acquired | 280985 | 42-417-36434 | DRILL | NAIL "135" | SHACKELFORD | 1985-07-24 | from: MIDWOOD PETROLEUM INC. |
Permit Activity
No data available