SHACK, BILL inactive
OP #767990 · Since 1983-05-31· P-5: Active
BOX 7, ALBANY
Spud Rate
71%
5 of 7 (6mo+)
Median Spud Days
344
p25-p75: 108-404d
Cancel Rate
0%
0 cancelled
Expired Undrilled
2
Avg Permits / Yr
0
Spud Momentum: inactive ⓘBased on wells spudded in the last 6 months compared to the prior 6 months. Active Years: 22 Horizontal: 0% Top County: THROCKMORTON
Window: | Type:
Permits (1yr)
0
vs Prior
0%
Counties (1yr)
0
Avg Depth (1yr)
--
Hz % (1yr)
0%
All Time
7
Basins (1yr): Eagle Ford / Maverick
Depth Range (1yr): 980 - 1,200 ft
Current Portfolio (RRC scheduling system)
Total Wells
1
On Schedule
0
Producing
0
Shut In
0
Acquired
1
from other operators
Divested
6
to other operators
Counties
THROCKMORTON 1
Fields
MCKEICHAN (STRAWN) 1
Cum Oil: 21,047 BBL Cum Gas: 0 MCF
Wells Operated (1)
| API | LEASE | FIELD | COUNTY | STATUS | SCHED |
|---|---|---|---|---|---|
| 42-447-05423 | ANDRADE | MCKEICHAN (STRAWN) | THROCKMORTON | — | N |
Production History
Permit History (all operated wells, latest 15)
View all →| SOURCE | PERMIT | API | TYPE | LEASE | COUNTY | ISSUED | FROM/TO |
|---|---|---|---|---|---|---|---|
| divested | 549580 | 42-447-36133 | DRILL | DAWS, MARGARET M. | THROCKMORTON | 2004-08-23 | to: S2 OIL LLC (1) |
| divested | 512451 | 42-417-38338 | DRILL | WALKER-BUCKLER "136" | SHACKELFORD | 2001-08-24 | to: SHACK BILL |
| divested | 501354 | 42-447-30153 | RENTR | DAWS, M. -F- | THROCKMORTON | 2000-11-16 | to: S2 OIL LLC (1) |
| divested | 495351 | 42-447-35992 | DRILL | DAWS | THROCKMORTON | 2000-05-24 | to: S2 OIL LLC (1) |
| divested | 480703 | 42-447-35903 | DRILL | DAWS | THROCKMORTON | 1998-12-01 | to: S2 OIL LLC (1) |
| acquired | 457339 | 42-447-05423 | RENTR | ANDRADE | THROCKMORTON | 1997-01-27 | from: GOOPCO, INC. |
| divested | 452217 | 42-447-35651 | DRILL | DAWS | THROCKMORTON | 1996-09-12 | to: S2 OIL LLC (1) |
Permit Activity
No data available