SHACK, BILL inactive

OP #767990 · Since 1983-05-31· P-5: Active

BOX 7, ALBANY

Spud Rate

71%

5 of 7 (6mo+)

Median Spud Days

344

p25-p75: 108-404d

Cancel Rate

0%

0 cancelled

Expired Undrilled

2

Avg Permits / Yr

0

Spud Momentum: inactive Active Years: 22 Horizontal: 0% Top County: THROCKMORTON
Window: | Type:

Permits (1yr)

0

vs Prior

0%

Counties (1yr)

0

Avg Depth (1yr)

--

Hz % (1yr)

0%

All Time

7

Basins (1yr): Eagle Ford / Maverick
Depth Range (1yr): 980 - 1,200 ft

Current Portfolio (RRC scheduling system)

Total Wells

1

On Schedule

0

Producing

0

Shut In

0

Acquired

from other operators

Divested

6

to other operators

Counties

THROCKMORTON 1

Fields

MCKEICHAN (STRAWN) 1
Cum Oil: 21,047 BBL Cum Gas: 0 MCF

Wells Operated (1)

APILEASEFIELDCOUNTYSTATUSSCHED
42-447-05423ANDRADEMCKEICHAN (STRAWN)THROCKMORTONN

Production History

Permit History (all operated wells, latest 15)

View all →
SOURCEPERMITAPITYPELEASECOUNTYISSUEDFROM/TO
divested54958042-447-36133DRILLDAWS, MARGARET M.THROCKMORTON2004-08-23to: S2 OIL LLC (1)
divested51245142-417-38338DRILLWALKER-BUCKLER "136"SHACKELFORD2001-08-24to: SHACK BILL
divested50135442-447-30153RENTRDAWS, M. -F-THROCKMORTON2000-11-16to: S2 OIL LLC (1)
divested49535142-447-35992DRILLDAWSTHROCKMORTON2000-05-24to: S2 OIL LLC (1)
divested48070342-447-35903DRILLDAWSTHROCKMORTON1998-12-01to: S2 OIL LLC (1)
45733942-447-05423RENTRANDRADETHROCKMORTON1997-01-27from: GOOPCO, INC.
divested45221742-447-35651DRILLDAWSTHROCKMORTON1996-09-12to: S2 OIL LLC (1)

Permit Activity

No data available
Live © 2026 Petrora