TINTOP OIL & GAS CO inactive
OP #860780 · Since 1985-08-16· P-5: Active
P O BOX 10387, FORT WORTH
Spud Rate
0%
0 of 3 (6mo+)
Median Spud Days
--
Cancel Rate
0%
0 cancelled
Expired Undrilled
3
Avg Permits / Yr
3
Spud Momentum: inactive ⓘBased on wells spudded in the last 6 months compared to the prior 6 months. Active Years: 1 Horizontal: 0% Top County: PALO PINTO
Window: | Type:
Permits (1yr)
0
vs Prior
0%
Counties (1yr)
0
Avg Depth (1yr)
--
Hz % (1yr)
0%
All Time
3
Basins (1yr): Eagle Ford / Maverick
Depth Range (1yr): 600 - 4,841 ft
Current Portfolio (RRC scheduling system)
Total Wells
3
On Schedule
0
Producing
0
Shut In
0
Acquired
3
from other operators
Divested
2
to other operators
Counties
THROCKMORTON 2
SHACKELFORD 1
Fields
C.D. (COOK SAND) 1
C.D. (TANNEHILL) 1
SHACKELFORD COUNTY REGULAR 1
Wells Operated (3)
| API | LEASE | FIELD | COUNTY | STATUS | SCHED |
|---|---|---|---|---|---|
| 42-417-36208 | DILLER B | SHACKELFORD COUNTY REGULAR | SHACKELFORD | — | N |
| 42-447-34332 | HARGROVE | C.D. (COOK SAND) | THROCKMORTON | — | N |
| 42-447-34333 | HARGROVE | C.D. (TANNEHILL) | THROCKMORTON | — | N |
Production History
Permit History (all operated wells, latest 15)
View all →| SOURCE | PERMIT | API | TYPE | LEASE | COUNTY | ISSUED | FROM/TO |
|---|---|---|---|---|---|---|---|
| divested | 300778 | 42-447-34589 | DRILL | BAILEY, C. | THROCKMORTON | 1986-04-08 | to: M. & K. DEVELOPMENT CO. |
| divested | 282635 | 42-367-32936 | DRILL | SCHULTZ | PARKER | 1985-08-16 | to: B & H GAS INC. |
| acquired | 268431 | 42-417-36208 | DRILL | DILLER -B- | SHACKELFORD | 1985-03-04 | from: CARTER DEVELOPMENT |
| acquired | 265960 | 42-447-34332 | DRILL | HARGROVE | THROCKMORTON | 1985-02-05 | from: CARTER DEVELOPMENT |
| acquired | 265961 | 42-447-34333 | DRILL | HARGROVE | THROCKMORTON | 1985-02-05 | from: CARTER DEVELOPMENT |
Permit Activity
No data available