42-059-31092
SHUT INBOOTH J.W.
CALLAHAN County · District 7 · SEQUOIA NATURAL GAS INC. · BOOTH (CADDO)
Permits
3
Max Depth
4,066 ft
First Permit
1979-11-16
Latest Activity
1989-09-22
Lifespan
10 yrs
Regulatory Status
Schedule
ON SCHEDULE
Completion
1989-08-24
Shut-In
—
Plugged
—
P-5 Org Status: Delinquent
!
EWA / Production operator mismatch
Scheduling: SEQUOIA NATURAL GAS INC. ≠ Production: MID TEXAS NATURAL GAS (reported 2007-07)
!
EWA / Permit operator mismatch
Scheduling: SEQUOIA NATURAL GAS INC. ≠ Permit: JONES CO.
Resolved via: scheduling → SEQUOIA NATURAL GAS INC.
Production Summary
Cum Oil
— bbl
Cum Gas
— mcf
First Production
1993-01
Last Production
2026-03
Operator History
Chain of Custody
Lease Production
Production is reported at the lease level. View production data, decline curves, and history on the lease page.
Permit History (3)
Permit Applications (3)
#364149 A JONES CO.
received 1989-09-20
#88946 A JONES CO.
received 1980-08-07
#64011 A JONES CO.
received 1979-11-16
Well Details
- Well Number
- 2
- Max Depth
- 4,066 ft
- Drill Type
- Vertical
- County
- CALLAHAN
- District
- 7
- Operator
- SEQUOIA NATURAL GAS INC.
- Completed
- 1989-08-24
Operator
- Location
- ALBANY
- P-5 Status
- Y (filed 2025-12-04)
- Cum Oil (all leases)
- 9,861 bbl
- Cum Gas (all leases)
- 331,686 mcf
- Activities
- OPRS/G, OPRS/O
- Total Permits
- 3