42-367-31085
DILL UNIT
PARKER County · District 7 · MKS CONSULTING CORPORATION · CABBAGE PATCH (BIG SALINE)
Permits
1
Max Depth
5,675 ft
First Permit
1978-04-17
Latest Activity
1978-04-17
Lifespan
< 1 yr
Regulatory Status
Schedule
OFF SCHEDULE
Completion
1982-12-29
Shut-In
—
Plugged
1996-03-14
EWA / Production operator mismatch
Scheduling: MKS CONSULTING CORPORATION ≠ Production: DYNAMIC PRODUCTION, INC. (reported 1995-01)
EWA / Permit operator mismatch
Scheduling: MKS CONSULTING CORPORATION ≠ Permit: RAW ENERGY CORPORATION
Resolved via: scheduling → MKS CONSULTING CORPORATION
Production Summary
Cum Oil
— bbl
Cum Gas
— mcf
First Production
1993-01
Last Production
1996-10
Operator History
originally filed by RAW ENERGY CORPORATION — asset transferred
Lease Production
Production is reported at the lease level. View production data, decline curves, and history on the lease page.
Permit History (1)
Permit Applications (1)
Well Details
- Well Number
- 1
- Max Depth
- 5,675 ft
- Drill Type
- Vertical
- County
- PARKER
- District
- 7
- Operator
- MKS CONSULTING CORPORATION
- Completed
- 1982-12-29
Operator
- Name
- MKS CONSULTING CORP
- Location
- WEATHERFORD
- P-5 Status
- Y (filed 2005-06-10)
- Cum Oil (all leases)
- 6,944 bbl
- Cum Gas (all leases)
- 7,666,510 mcf
- Total Permits
- 6