42-497-32567

Final Completion

WOOTEN

WISE County · District 9 · DALLAS ROYALTY INC. · BOONSVILLE (BEND CONGL. GAS)

RRC Lookup

Permits

1

Max Depth

5,838 ft

First Permit

1983-05-10

Latest Activity

1983-05-10

Lifespan

< 1 yr

Regulatory Status

Schedule

OFF SCHEDULE

Completion

1984-02-15

Shut-In

Plugged

2000-06-08

!

EWA / Permit operator mismatch

Scheduling: DALLAS ROYALTY INC. ≠ Permit: GO OIL CORP.

Resolved via: schedulingDALLAS ROYALTY INC.

Production Summary

Cum Oil

bbl

Cum Gas

mcf

First Production

1993-01

Last Production

2000-11

Operator History

originally filed by GO OIL CORP. — asset transferred

Lease Production

Production is reported at the lease level. View production data, decline curves, and history on the lease page.

Permit Applications (2)

#194293 A GO OIL CORP.
received 1985-04-12
#194293 A GO OIL CORP.
received 1983-05-10

Well Details

Well Number
1
Max Depth
5,838 ft
Drill Type
Vertical
County
WISE
District
9
Completed
1984-02-15

Operator

Location
JACKSBORO
P-5 Status
Y (filed 2012-12-07)
Cum Oil (all leases)
41,582 bbl
Cum Gas (all leases)
11,263,852 mcf
Total Permits
17

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