FARRINGTON ENGY INC inactive

OP #263540 · Since 1980-04-30· P-5: Active

P.O. BOX 130234, TYLER

Spud Rate

27%

3 of 11 (6mo+)

Median Spud Days

21

p25-p75: 14-26d

Cancel Rate

0%

0 cancelled

Expired Undrilled

8

Avg Permits / Yr

2

Spud Momentum: inactive Active Years: 7 Horizontal: 0% Top County: WOOD
Window: | Type:

Permits (1yr)

0

vs Prior

0%

Counties (1yr)

0

Avg Depth (1yr)

--

Hz % (1yr)

0%

All Time

11

Basins (1yr): East Texas, Eagle Ford / Maverick
Depth Range (1yr): 1,000 - 12,000 ft

Current Portfolio (RRC scheduling system)

Total Wells

5

On Schedule

0

Producing

0

Shut In

0

Acquired

from other operators

Divested

3

to other operators

Counties

WOOD 5

Fields

QUITMAN (Q5 SW) 3
QUITMAN (EAGLE FORD) 1
QUITMAN (Q5 S.E.) 1

Wells Operated (5)

APILEASEFIELDCOUNTYSTATUSSCHED
42-499-30137GRAHAM DANQUITMAN (Q5 S.E.)WOODN
42-499-30760GRAHAM DANQUITMAN (Q5 SW)WOODN
42-499-30870GRAHAM L.R. ET ALQUITMAN (EAGLE FORD)WOODN
42-499-31032THOMAS ANNIEQUITMAN (Q5 SW)WOODN
42-499-30808THOMAS/MCINTOSH WATERFLOODQUITMAN (Q5 SW)WOODN

Permit History (all operated wells, latest 15)

View all →
SOURCEPERMITAPITYPELEASECOUNTYISSUEDFROM/TO
divested32452242-499-31523DRILLGRAHAM, DANWOOD1987-01-12to: BIG RUN PRODUCTION COMPANY
divested32452242-499-31523DRILLGRAHAM, DANWOOD1987-01-12to: BIG RUN PRODUCTION COMPANY
divested24524742-499-31277DRILLCATHEY, L. B. ET ALWOOD1984-07-18to: FARRINGTON ENERGY INC.
divested22677042-459-30614DRILLF.E.I. L.M. BAIN G.U. #1UPSHUR1984-01-12to: ARCADIA REFINING CO.
filed13500242-499-31032DRILLTHOMAS, ANNIEWOOD1981-09-30
filed9811242-499-30870DRILLGRAHAM, L.R. ET ALWOOD1980-11-06
filed7975642-499-30808DRILLMCINTOSH, OPALWOOD1980-04-30
6821642-499-30760DRILLGRAHAM, DANWOOD1979-12-31from: FARRINGTON, WALTER L., JR.

Permit Activity

No data available
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