42-499-31523
Final CompletionGRAHAM DAN
WOOD County · District 6 · BIG RUN PRODUCTION COMPANY · QUITMAN-MCINTOSH (WOODBINE)
Permits
2
Max Depth
4,500 ft
First Permit
1987-01-12
Latest Activity
1987-01-12
Lifespan
< 1 yr
Regulatory Status
Schedule
OFF SCHEDULE
Completion
1989-04-19
Shut-In
—
Plugged
2006-03-16
!
EWA / Permit operator mismatch
Scheduling: BIG RUN PRODUCTION COMPANY ≠ Permit: FARRINGTON ENERGY INC.
Resolved via: scheduling → BIG RUN PRODUCTION COMPANY
Production Summary
Cum Oil
— bbl
Cum Gas
— mcf
First Production
1993-01
Last Production
2008-03
Operator History
originally filed by FARRINGTON ENERGY INC. — asset transferred
Lease Production
Production is reported at the lease level. View production data, decline curves, and history on the lease page.
Permit History (2)
Permit Applications (2)
#324522 A FARRINGTON ENERGY INC.
received 1987-03-24
#324522 A FARRINGTON ENERGY INC.
received 1986-12-18
Well Details
- Well Number
- 5
- Max Depth
- 4,500 ft
- Drill Type
- Vertical
- County
- WOOD
- District
- 6
- Operator
- BIG RUN PRODUCTION COMPANY
- Completed
- 1989-04-19
Operator
- Name
- BIG RUN PROD CO
- Location
- KILGORE
- P-5 Status
- Y (filed 2025-05-02)
- Cum Oil (all leases)
- 562,969 bbl
- Cum Gas (all leases)
- 6,234,116 mcf
- Activities
- G/PUR, OPRS/G, OPRS/O
- Total Permits
- 23